双芯铜导体架空绝缘导线的不良现象分析与控制优化

    Analysis and Control Improvement of Poor Phenomena of Double Core Copper Conductor Overhead Insulated Wire

    • 摘要: 针对双芯铜导体架空绝缘导线生产过程中出现的导体跳股、电阻波动及绝缘偏芯等质量问题,文中通过优化拉丝、绞线和绝缘三大关键工序进行优化改进。在拉丝工序中,通过启用在线退火系统将铜丝抗拉强度控制在405~450 N·mm−2范围,并调整铜丝直径至1.33~1.34 mm,解决了因铜丝硬度过高导致的跳股问题。在绞线工序中,将首道模具改进为7孔约束结构,并匹配分线板与模具的夹角,显著减少了绞合过程中的铜丝硬化问题。在绝缘工序中,通过增加长度为35 mm的模芯定位区,并调整中心距为6.6 mm,有效消除了绝缘层偏芯及最薄点不达标的现象。经优化后试生产及性能验证,结果表明:导体拉断力达3.807 kN,20 ℃导体电阻降至1.887 Ω·km−1,绝缘最薄点提升至0.86 mm,产品外观与尺寸均符合要求。该方案可为多芯铜导体架空绝缘导线的生产提供技术参考。

       

      Abstract: To address quality issues such as conductor strand jumping, resistance fluctuation, and insulation eccentricity in the production of dual-core copper conductor overhead insulated wires, key process optimizations were implemented across wire drawing, stranding, and insulation extrusion. In the drawing process, the online annealing system was activated to control the tensile strength of copper wires at 405~450 N·mm−2, with wire diameter adjusted to 1.33~1.34 mm, resolving strand jumping caused by excessive hardness. For the stranding process, the first-stage die was redesigned into a 7-hole constrained structure, and angles between the wire separator and dies were matched, significantly reducing work hardening. In the insulation process, the die core sizing zone length was increased to 35 mm and the center distance adjusted to 6.6 mm, effectively eliminating insulation eccentricity and substandard minimum thickness points. Post-optimization trial production showed: conductor tensile breaking force reached 3.807 kN, DC resistance at 20 ℃ decreased to 1.887 Ω·km−1, and insulation minimum thickness improved to 0.86 mm. All dimensional and appearance criteria were met. This optimized approach provides a reliable technical reference for producing multi-core copper conductor overhead insulated cables.

       

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